All posts by Simon

A new Honigkuchen recipe

A new recipe for delicious christmas cookies, called, “Honigkuchen”, say, honey cookies:

Prepare a mixure of 250 g wheat flour, 100 g rye wholegrain flower, 15 g christmas spices (anis, cinnamon, etc.), add,

300 g of honey – heat so that it is fully liquid but don’t boil

2.5 g potash (potassium carbonate), 5 g hirschhornsalz (ammonium bicarbonate) – dissolve these salts in about 10 mL of warm water (don’t worry if it doesn’t all full dissolve), add to the mixture.

Mix and kneed to a thorough dough, let it rest about 2 days at room temperature, well covered.

For cookies about 8 mm thick, then bake at 175°C for 15 minutes.

For a glossy surface you can paint them with condensed milk before baking.

Earlier recipe, here: Christmas Time: Honigkuchen (honey based cookies)

Bauhaus VoltoLux LED Lamp: a early failure sickness finally subsided

Some of the ceilings in my house have LED lights installed in false ceilings, a total of 45 led lamps of the same kind (GU10, 4 Watt reflector LEDs). These are of regular quality, sourced from Bauhaus, a normally trustworthy outlet. But certainly these LED lights cannot be trusted at all. Of the 45 pieces installed, already 4 failed in the first year – occasional use. And another one just failed recently.

The advantages claimed are various, long lifetime, rugged, etc., but Bauhaus doesn’t say that you need to buy 10% more lamps than you need, just to replace the early failing lights. Not even to mention about the effort or replacement, etc.

All of the LEDs are 25360318 with frosted front, 10 LED chips per piece. The failure mode is normally intermittent, so the LED will come on for a little, then go off, it may also come on after a little while, unpredictable.

As it turns out, these LEDs are actually repairable, but removing the front glass disc (frosted diffusor), which is done by heating it for a little while with hot air at about 200°C. The front disc seems to have fixed with some epoxy glue.

Poking around, it becomes clear that the failure more is a broken interface between one of the LED chips, and the aluminum heat-conducting round board they have been soldered to. So, either the design has some flaw, or there are thermal issues or solder/flux issues when manufacturing. Shock or vibration effects can be excluded, because these lights have ever since the renovation been mounted in the ceiling, with no touch or vibration.

To fix it, I just re-flowed the solder, after applying a little flux, and the issue went away. Now you can close the light again, using epoxy glue, and it may provide some further service. No statistics yet on the lifetime of repaired LEDs.

In any case, buyer beware of any of the praised LED lamps, many may fail on you well before their expected lifetime ends, better keep all receipts, so that you can have them replaced by the Bauhaus hardware store, or wherever you prefer to buy your lighting supplies.

HP 4192A LF Impedance Analyzer: another visit to the workshop

The analyzer, I had fixed it 3.5 years back, see HP 4192A LF Impedance Analyer, the instrument has been back to very good shape, and since then been operated at an university overseas. Recently, I got the message that repair is needed, the instrument didn’t start up.

I tried hard to fix it remotely, because of the significant size and shipment cost, and the general risk of shipping such precision gear around the world. But to no avail, the failure seemed to complex to repair by remote instructions.

First difficulty, to get the instrument shipped to Germany, and to get it through customs – quite a task that took several hours, personal appearance at the customs office, and some paperwork, along with a small fee.

Following the old rule, to check the powers supply first, it was quickly seen that there is a short on the -15 rail, and systematically unplugging the assemblies, quickly found the short on the A3 assembly plug, which is also powering the A1 assembly – the location of the actual fault.

Smell and eye are the best methods… to find easy faults.

Once you know the location, easily seen – the burned inductor. I replaced it by a 4.7 µH inductor I had around, and fitted a new capacitor (tantalum cap).

The NEC-branded cap was dead-short.

Now, the instrument powered up, at least the power supply, but no further sign of life. Checked around the CPU board, and strangely, even the first test showed, no clock! the CPU clock is derived from the A3 master oscillator, by a divider chain – and probing there, no signal on the 1 MHZ or 100 kHz lines either.

The diver chain uses various divide-by-2, 74C74 flip-flops.

Hard to see, but to determine the defective chip, I cut the clock pin at the 74C74, because the clock was low. So I was not sure if the clock generator/amplifier was defective, or just overloaded by the 74C74.

With no 74S74 (guaranteed to run at 75 MHz, typically up to 115 MHz clock) at hand, I replaced it by a 74F74 (which easily handles the 40 MHz clock).

Interestingly, both 74S74 (HP part 1820-0693) had failed. Maybe both were suffering from some transient when the power supply sorted. We may never find out.

Finally, I noticed some unreliable switch-on characteristics that could be traced to some flaky resistors on the power supply board – this board had corrosion issues that damaged some resistors.

A little box of replaced parts… not too many.

Finally, put the instrument to a 24 hours tests, and also run some calibration of DC bias, which had drifted a little. Otherwise all well in spec and well tuned.

Packing it all up: this time, a package to Saudi-Arabia. The instrument wrapped in bubble wrap, then a layer of styrofoam, then a wooded box re-inforced with metal parts and screws, and a cardboard layer all around (without cardboard, DHL will rank it as “special handling”, at a significant additional charge).

After about 2 weeks, the instrument safely arrived in Saudi, and it is indeed working again. Recipient is happy, me too!

Metalworking: strange defects of long-used tools

Recently, I found two strange defects in my workshop, noteworthy to write it down.

Ever since I expanded my workshop I notices some losses of compressed air, i.e., when coming back after a business trip, the pressure of the compressed air pipework is down from normally 6.5 bars, to only 2-3 bars, or even less after a longer vacation. I had attributed it to some leaking air gun or something like that, but finally I did a search and found various leaks at one distribution point.

(1) the water mist filter had a leak at the drain valve — fixed it by closing it altogether. There is not too much water collected, it is installed only to avoid dust and such getting into the system further downstream.
(2) one of the fitting was leaking, because strangely there are some air fittings available that neither have a seal surface, nor conical thread, to it is hard to get it tight by tread tape in the first place (sometime I resorted to gluing-in those fittings with Epoxy glue).
(3) Still, when checking with some soapy water – bubbles at the distribution fitting (5 connections 1/2″). Strange, strange, strange.

Clearly, a defective casting with a hairline crack leak. Maybe the temperatures or the mold or the liquid brass were not right, or the pouring wasn’t steady enough.

The defect line goes all around the fitting, otherwise I would have tried to file it out and solder it tight. Anyway, it is not worthwhile to fix such part at the risk of it failing again. So I replaced it with a new fitting at the cost of EUR 9.90 and at least 3 hours of work to get it all investigated, replaced, fitted and leak tested. Maybe a good idea to fully upgrade the pressurized air system of my workshop, which is now a combination of various distribution pieces, hoses, connectors. But there are trade-offs of perfection, cost, and efficiency — I have actually installed some air pressure distribution pipes for others (like, polyamide pipe, PE-Al composite pipe), but at my own workshop, I will be dealing with a less perfect system, at least, the major leaks have now been found and eliminated.

Another instance of strange failures, I noticed some problems with a bench vice, the smaller size vice I use regularly, and have been using since my childhood. If I remember right, I bought it for something like 35 Deutschmarks way back around ~1990. After all these years, it had some failures, the spindle pin sheared off once (maybe because I tightened it too much), and also a retaining piece of the front part of the spindle wore out (probably very soft steel and insufficient lubrication). Also some part of the casting broke off before, circled in black. Now, I almost injured myself as a part came loose unexpectedly, finally, as they say, always check the tool before you use it.

Didn’t need to go far, a major crack of the dovetail guideway.

It is cracked through, but holding on enough so that the defect is not easily seen without disassembly.

Finally, a cast iron bench vice, after 33 years of service (not always careful use), it may eventually break.

For replacement, I wanted a slightly bigger bench vice, 115 mm width. Also, a solid steel vice that is not too bulky and has a strong grip. These don’t come cheap, but I found a good (but rusty) Peddinghaus Matador steel vice for 35 EUR used, listed in online adds.

After some cleaning, adjustment, and other TLC, it is installed on the bench and working great. Definitely a step up.

Meridian 506 CD Player: after 5 years, in need for more attention

Recently, I had two instances of equipment coming back after some year – with different defects that at their first visit in my workshop. One device is the Meridian 506, a high-class CD player that is popular with hifi enthusiasts, and has been marketed for many years in various different versions. Earlier I had fixed some design issues with the motor driver of the CD deck, see Meridian 506 CD Player: a hot driver.

This time, it wouldn’t detect any CDs, and made some noises. The deck was still opening fine. After looking around, there is no obvious defect, the power supplies are good. All the service modes work – just that I can’t get it read discs or even lock on tracks, it just spins up, then stops.

Reading through all various posts, it seems clearly related to the CD head assembly, this version of the 506 uses a CDM 4/19 Philips laser head assembly, and these are known to wear out over time, i.e., the laser will show aging, and then the mechanism can’t lock on the CD.

Well, easy enough, I found a CD 480 player cheaply as used goods, and this has the desired CDM 4/19.

It arrived strangely packed, but well, better strangely packed than insufficiently packed. Indeed, a lot of styrofoam, chips and paper inside.

Inside, a very simple assembly, much lighter than the Meridian deck. Just some thin plastic.

Easily disassembled the donor.

There are some changes necessary – the hub is different, but can be removed with simple tools (plastic tools) and switched.

Well, all this done, unfortunately —– no success. Still same symptoms. Next, poking around the main TDA chip, there are no signals that are of any use. Strange. Normally it should at least start reading and locking, but it doesn’t (not that the CD drive uses a feedback loop to keep the head on the track, by adjusting the laser arm coil current according the the laser feedback; in these drives, the laser arm is driven by a coil).

After some further study, finally realized that the CD is spinning the wrong way. How can that be? Seems like a defective motor driver! On the small board of the CD deck, there are two L272, and one of them is terribly hot. Not good.

The L272 has long been obsolete, but I would two pieces cheaply on a Chinese website, these were apparently no new but recovered from used equipment. Well, no problem, I rather buy used parts than fake parts.

With these repairs done (not easy because the soldering of the L272 is very strong, need to put a lot of heat to the small board because all the ground pins are firmly connected to a ground plane), the Meridian is working great again, let it play for several hours with no skipping.

And, we now still have a spare laser head assembly should it fail next.

Another Micro-Tel 1295 Precision Attenuation Measurement Receiver: irresistible green

I am trying hard to resist the temptation of buying more test equipment, but the Micro-tel special green color has a hypnotic effect on me, and combined with the right price, I could not resist to buy one more Micro-tel 1295 receiver. These are very capable 0.01~40 GHz fundamental-mixing receiver (fundamental mixer until 18 GHz, above that, harmonic mixer), with very large range, like, 120 dB, and 0.001 dB attenuation resolution. Ideally suited to calibrate attenuators or to check antennas, etc.

The unit – offered as non-working – arrived very well packed. Unfortunately, many people send sensitive equipment in some thin cardboard boxes. This particular equipment cost close to 85 kEUR in 1989, plus mixers. Also, it has long been under export control from the US, because of its unique range and accuracy.

Bubble wrap, other fibre wrap inside.

Finally all in foil.

The defect, it doesn’t show any reading on the display, and both the HI and LO leds are on, which is abnormal. The 1295 has a 12 dB range bolometer detector, any signal below 0.5 dB or above 12.5 dB will light up the LO or HI lamp, and you would need to select another 10 dB step of the IF attenuator (a high precision 30 MHz attenuator), or let the automatic attenuation selector do the job.

There are many boards inside, but all nicely numbered and with instructions in the manual.

The HI and LO level detection is done on the A3B2 assy.

According the the schematic, U2, a MC1458 generic dual opamp is switching the LEDs and providing signals to drive the automatic attenuation selector.

A quick check revealed that U2 is defective, so I replaced it quickly, and this already solved the issue and brought back the display.

Another trouble related to unstable lock of the 2.3 GHZ auxiliary LO that is used for the 0.01-2 GHz range (which uses a two-stage down mixing).

Fortunately, I had a spare 2.3 GHz from my parts unit (which I bought years ago – a partial unit – while I was living in the US). That part was missing one of its covers, and had also some issues earlier, but I had fixed it a while back just for curiosity. Now I can fix the unstable 2.3 GHz removed from the unit during next winter. It has a 2.3 GHz VCO, a 100 MHz local oscillator and a PLL inside.

After calibrating all the oscillator frequencies, which went without trouble, I noticed that the top 120 dB attenuator was 0.04 dB off, well, not a big deviation, but I would rather have the unit working perfectly. So I removed the attenuator for further study.

It is build with really high quality relais, more than USD 50 (each!!), and some precision resistors.

Nothing could be found wrong with the unit by visual inspection.

Also I used the VNA to check the attenuator, and all seems well working.

All the 3 segments, virtually equal at 10 dB each.

Finally, I put everything back together, a little clueless, but, now, for some reason, all is working and stable. Maybe it was some lose connector, or other strange effect that is now gone. All attenuators calibrated perfectly, using by HP 3335A level generator (which has a top-accuracy attenuator).

Finally the 1295, working just perfectly fine. Maybe better than ever before.

Interestingly, as with all of these Micro-tel devices, the side and top/bottom panels were painted with various kinds of special military paint – some with a rubberized paint that will dissolve into some gluey substance over time, some with a type of “abrasive” paint, other already re-painted in forest green.

The paint has very large and hard grit, almost like sandpaper. But I will leave it untouched, it seems the original looks for this serial number range (the 1295 seems to have been in production for 10+ years).

Now, a little gallery of all my Micro-tel 1295 receivers: the first two, part of my frequency-locked attenuator calibrator (can measure reflection and transmission at the same time).

One as part of an E-band (60-90 GHz down-converter).

Any now, already two spare units in perfect calibration.

Still, in the basement, a box of spares… likely I won’t run short of receivers soon. Maybe even buy another one should it come around.

Watkins-Johnson SE222-50 Backward Wave Oscillator: the magic helix

Recently, I got a Marconi Instruments Model 6651 RF Plug-in (26.5-40 GHz), for the 6600 sweep generator. These were basically the 1st generation sweep generators extending into the millimeter wave region.

A number of plug-ins were available, mostly based on Watkins-Johnson BWO (backward wave oscillators), which are a particular type of electron tube.

These sweepers were first introduced in the late 1960s, early 1970s. New plug-ins became available as development of BWOs and similar sources advanced.

I have no price list, but surely these items came at a hefty price tag in these early days, even not quite cheap today.

My unit had a pretty “new” 1990 date-code BWO, I expect, it had been replaced by its former university owner at least once, also the cables and connectors of the BWO looks newer compared to the rest of the plug-in. Because of their nature, the BWOs only have a limited life-time, a few 1000 hours at best.

There are numerous warning labels, because to focus the electron beam, a strong magnetic field is needed.

The output is a gold-plated waveguide flange, for Ku-band waveguides.

The general layout of a BWO: there is an electron gun, producing, in our case, a hollow electron beam, with the necessary heater, kathode, anode. Then, the helix, and the collector (which is basically at helix potential or a little bit higher, say, 100 volts higher. The helix voltage is quite high, for exmaple, 1~1.5 kV.

While there is no information from Watkins-Johnson available online for any of these devices, a lot can be learned from related Hewlett-Packard microwave sweeper plug-ins (8697A), where (arguable) the same or very similar BWO has been used (some HP units may use Varian BWOs).

Unfortunately, after quite some effort with high voltages and pretty dangerous tests, it became clear that the tube barely gave some power. Maybe, because it had not been operated for a long time (some people and datasheets say that the BWO should be run at last once every 6 months, or similar, to preserve its function…).

But anyway, I have other, more stable and easy to use sources for this range, so I didn’t want to scrap the BWO without having a closer look at this. When do you normally get a chance to check out the secret workings of such marvelous devices!

First things first, hidden inside a heavy magnet, silicon rubber, and a waveguide coupler: the tube. A very mysterious piece of engineering, only a few companies ever mastered to produce these.

Also by the numbers and hand-writing, pretty clear that these units were all hand-made and assembled by engineers and highly skilled people.

The mount is all gold plated, a tapered wave guide eventually bent by 90°, so the microwave radian can be coupled from a small gap in the silver coating of the tube, to the outlet. This tube was meant to generate about 10 dBm.

The helix at the collector end.

You can see, the helix is kept centered by 3 glass (quarz?) rods, these rods are just held in place by the tension of the helix, but normally won’t move during operation and shipment. Surely, will all the glass-metal interfaces, mounts and connection points, it is no good idea to drop these units – some interfaces may break, or mis-align beyond repair. Furthermore, several Watts of powder will need to be dissipated, calling for a reasonably elaborate design of the mount not only to conduct the microwave radiation from the tube to the output, but also to dissipate the heat from the collector and helix.

All the high voltage socket part is embedded in two layers of silicon rubber. First they put some denser rubber around the socket to fix everything in place, probably run some tests, and then sealed it all by filling the further space with some pretty soft, highly filled silicon rubber. What they didn’t consider – the cable also has silicon isolation, and deteriorates in contact with other silicon materials. This may be one of the reasons for the unstable operation, because some wires were pretty close and the isolation seems very brittle.

Furthermore, I did some measurements of the critical parts, just in case I would even want to fabricate own BWOs, at least I have some working dimensions to start with.

The helix is normally made from flat molybdenum strip. At the bottom (gun end) it is mounted to a small ring. Scale is 210 px per 1 mm, in case you want to take dimensions…

A typical power supply – I am thinking about building a BWO power supply for some other old BWOs I have around (for other frequency regions), but it is fairly involved – the old design used high voltage 2 kV transformer with further high-voltage stable windings to provide the collector offset voltage, several expensive high voltage capacitors, and high voltage regulation vacuum tubes. I think it will be a good challenge for winter to build a 2 kV regulated and low-ripple power supply, solid state, probably with some series-connected MOSFETs.

Any of such future supplies will need a pretty special plug: heater voltage, anode and cathode voltages, helix voltage, collector voltage. At least I can go without any analog linearization voltage, if I manage to make the helix supply digitally controllable.

Inside the 6651 plug-in the BWO is connected to the board with some screw terminals. Seems to work well even at the high voltages. Surely there is no touch protection for these devices, just a few warnings not to get too close!

Wood and Steel, covered in Paint: a new garden bench

Recently, some heavy metal work in the precision workshop. Amongst other projects, I decide to build a new bench, to set it up behind the workshop building, to enjoy warm evenings during summer. Surely you could buy a bench, but I wanted certain dimensions, in particular, flat and somewhat wider seat area. A rough sketch shows the main dimensions. A cushion can be added, it matches 200 cm wide, 50 cm deep size.

All is made from solid flat hot rolled steel, one piece bent (after heating it with an oxygen torch, and using a small bending fixture), the other pieces welded (TIG).

All the angles were nicely hit.

I made a full size template drawn on stiff cardboard, so the welding and alignment could be easily done, then, fine adjustment by using the electronic level.

To get the right angles I had a look at some benches in public parks, etc., better to compare new design and existing know-how!

The seat, a little inclination to make sure water will drain.

The wood, douglas fir, it has a fair amount of resin and is quite resistant against weathering. It may darken, but it is not prone to rotting. I painted it with some sun-protecting varnish, two layers.
My uncle kindly provided the wood, from my ancestors village, ready to use. Saved a lot of time, compared to cutting and preparing the wood with my humble small woodworking tools.

The metal parts, carefully removed the rolling scale, added rust-proofing primer, and then two layers of solvent based lacquer. You could also consider hot zinc treatment, but such solid steel, painted, should last a hundred years, or longer.

Finally, after some hours of work, and drying the varnish for 1 week during a business trip: finished and at its final place. Very comfortable!

HP 11517A aka 08747-60022 Harmonic Mixer: a little study of a very intriguing device

As part of a HP R8747A 26.5-40 GHz reflection/transmission test unit (for the 8411A network analyzer; 6300 USD in 1973 — about 40 kEUR today), I got two HP 08747-60022 harmonic mixers, one didn’t seem to work right, the diode has just 0.2 V voltage drop. These were fairly fragile devices, only designed for 1 mW of power, and very static sensitive, point contact devices.
In addition to the regular 11517A, the 08747-60022 has a bias connection (needs about 1.5 V DC bias, center positive).

The main unit can work from 12 to about 40 GHz, with a set of adaptor waveguides.

The unit can be taken apart, all precision machined.

The diode is pressed in, on some holder (haven’t tried to remove it from the case).

There are several other precision parts, a coaxial resistor, held on to the diode with a spring.

There is also a spacer, with a very flat capacitor, a DC block. The spacer is modified to connect the center conductor to a surface at the perimeter (used for DC bias).

Further up, there is a low-pass, machined from a single piece and gold plated.

The N-type connector, stainless, is screwed on.

The DC bias uses a small 1.5 kOhms resistor, and a custom connector, so that the resistor is pushed onto the spacers’s connection.

Here, a quick schematic. Seems a lot of engineering went into this device…

Finally, we need a microscope to study further here, the diode (the square), about 0.25 mm side length. It is isolated from the case by an air gap.

The diode is made by a contact junction, a small tungsten(?) whisker.

Probably, this whisker needed some adjustment during manufacturing. I tried to adjust it a bit, but this didn’t change the diode characteristics of my broken unit, unfortunately (anyway, these devices are more for study than for use; currently using only cartridge-based diode mixers).

Also, looking into the waveguide of the assembled mixer, with good long-range optics, I could get a shot of the actual point contact in action. Very interesting historic technology.

Spring repairs: Fixing and frost-proofing ball valve

Recently, I have been setting up the watering system for my vegetable garden again. In my area, the soil is a little sandy, not bad for growing vegetables because slugs and snails don’t like such soil, but surely it needs proper watering.
All in all it is about 200 meters of 16 mm drip irrigation pipe, 16 mm size, with drippers every ~33 cm, nominal 2.1 L/h each. The system is run at about 1.5 bar. Some specific plants like pumpkins and certain berry shrubs in other area of the garden have their own supply by 4 mm tubing and individual adjustable drippers.

In the past years, the system has severed me well, and just last year, I have upgraded the water supply by setting up a new well. So there is plenty of water, and every day, at least in summer, the system supplies about 400 L a day, in two portions (like, at 6:30 am and 6:30 pm). Glad I don’t have to carry all that water.

All the water system, pump and distribution piping had been empty over winter, to avoid frost damage to the pipes. I keep the ball valves at about 45° angle, but this year this didn’t help to prevent damage to one of the valves (all the other valves are OK).

It is a combined, low cost China-made ball valve with strainer, I bought two of these some years back.

It is tight when closed, but when opened, water comes out at the crack indicated in the picture.

How can this have frost damage? Well, with the pipe empty, it should be safe? There is considerable dead space in this valve, the ball also has an indentation (cut-out) at the side opposite to the handle. It is brass, chromium plated.

As luck would have it, I had the second valve still in a box, it had been in service for some years until someone broke-off the handle (never throw away parts that may be suitable as spare part donor…). Surely it would be quick to just replace it, potentially, even with a better quality ball valve, etc., but why now study it and fix it?

Breaking open the valve, the two parts are screwed together fairly hard, and glued with some kind of epoxy or similar glue.

But nothing that can withstand a large spanner and a pipe wrench! So, the front part with the PTFE seal looks good. Also the spare valve (with the handle missing/broken off) was disassembled in no time.

Now, how to frost-proof ball valves? It is quite easy, and a well-known trick. Just dill a hole, about 3-4 mm in the far side (low pressure side) of the ball, then it will drain the dead space, when left open (or at an angle).

It is essential to remove any burrs, so I countersunk the hole, and polished the edge with some find sandpaper.

Everything put back together, I used some acrylic compound to seal and tighten the screw threads of the two-part valve. Good as new!